North Sea Norway 1989 |
Problem: During the drilling of a potential production zone with a near balanced condition, a simultaneous lost circulation and influx scenario occurred. After several days of attempting to kill the well, a backoff/sidetrack was planned. Wireline tools became stuck inside the drillpipe during the backoff operation. Well control was lost during a subsequent coiled tubing clean out operation on this North Sea HPHT well. Ultimately, the drillpipe had to be sheared leaving 4500 m of coil tubing inside the drillpipe. The wellhead pressure increased to over 10,000 psi, resulting in an underground blowout. |
Remedial Strategy: A surface re-entry project utilizing a high pressure riser and snubbing unit (contracted and supervised by Boots & Coots) would be used in combination with a simultaneous relief well to regain control of the blowout. The relief well surface location was positioned 1100 m away and would intersect the open blowout wellbore below the bit, at a depth of 4705 m tvd. Heavy mud would ultimately be circulated by the relief well and monitored by the surface re-entry operation. A direct hit of the wellbore was necessary due to low fracture strength. | |
Special Services: John Wright Company (JWCO) was contracted near the end of the project through Boots & Coots to supervise the special services required for this project. Services provided included pre-planning and on-site supervision of directional drilling, surveying, and casing detection. Vector Magnetics, responsible for electromagnetic ranging, was coordinated through JWCO and worked together as one team. | |
Challenges: The project
was complicated by the following:
|
|
Results:
|
|